Flow field survey in a transonic compressor rig

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Authors
Rose, Christopher W.
Subjects
Advisors
Hobson, Garth V.
Date of Issue
2006-06
Date
Publisher
Monterey California. Naval Postgraduate School
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Abstract
As the Navy prepares to transition to F-35C Joint Strike Fighter the need to understand "pop stalls-- caused by steam leakage in catapult systems is of concern. â Pop stalls* caused by steam ingestion through the aircraft engine result in a loss of power and possible engine stall. The F-35C is a single engine aircraft and therefore the probability of a â pop stall* resulting in the loss of the aircraft is increased. Investigation of this phenomenon is currently being examined at the Turbopropulsion Laboratory by means of a transonic compressor rotor. The present study utilizes both three and five-hole probes to survey the flow field upstream and downstream of the rotor to examine compressor stability. A new compressor performance map was defined and a validation of previous steam ingestion was performed.
Type
Thesis
Description
Series/Report No
Department
Organization
Naval Postgraduate School (U.S.)
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NPS Report Number
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Format
xiv, 53 p. : col. ill. ;
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Distribution Statement
Approved for public release; distribution is unlimited.
Approved for public release; distribution is unlimited.
Rights
This publication is a work of the U.S. Government as defined in Title 17, United States Code, Section 101. Copyright protection is not available for this work in the United States.
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